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Performance improvement of biomass cogeneration plant by dual loop organic Rankine cycle (CROSBI ID 631546)

Prilog sa skupa u zborniku | ostalo | međunarodna recenzija

Lončar, Dražen ; Guzović, Zvonimir ; Šerman, Nikola ; Performance improvement of biomass cogeneration plant by dual loop organic Rankine cycle // Chemical Engineering Transactions, Volume 39, Special Issue / Varbanov, P.S., Klemeš, J.J., Liew, P.Y., Yong, J.Y. (ur.). Prag: Italian Association of Chemical Engineering (AIDIC), 2014. str. 367-372

Podaci o odgovornosti

Lončar, Dražen ; Guzović, Zvonimir ; Šerman, Nikola ;

engleski

Performance improvement of biomass cogeneration plant by dual loop organic Rankine cycle

Biomass cogeneration plants in wood industry are usually designed to cover large share of site heat demand. However, plant capability to cover peak load in winter could lead to low utilisation of installed capacities at sites whit high seasonal heat demand fluctuations. At some sites, where income of sold electricity is essential for plant investment payback, non- cogeneration operation mode is applied and evacuation of surplus heat through air cooled heat exchangers is usual practice. Price increase of wood chips, as a consequence of increased demand, accompanied by implementation of sustainability criteria for biomass utilisation forced plant owners to reconsider existing business model and to find more efficient ways of biomass utilisation. Based on analysis of operational pattern of existing 1 MW organic Rankine cycle plant in wood pellets processing industry in Croatia, configuration and parameters of an additional low temperature organic Rankine cycle have been investigated in order to find technically and economically optimal configuration. Taking into account time dependant variation of surplus heat of the high temperature cycle in the range of 1 to 3 MW and variation of ambient temperature, net output power of the low temperature cycle has been optimised. Off- design and part-load operating conditions have been also considered and results of analyses have been presented.

low temperature ORC; second loop; biomass power plant

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Podaci o prilogu

367-372.

2014.

objavljeno

Podaci o matičnoj publikaciji

Chemical Engineering Transactions, Volume 39, Special Issue

Varbanov, P.S., Klemeš, J.J., Liew, P.Y., Yong, J.Y.

Prag: Italian Association of Chemical Engineering (AIDIC)

978-88-95608-30-3

2283-9216

Podaci o skupu

Modelling and Optimisation for Energy Saving and Pollution Reduction, PRES 2014

predavanje

23.08.2014-27.08.2014

Prag, Češka Republika

Povezanost rada

Strojarstvo